
In the Event of a Water Landing tells for the first time
the full stories of the Bermuda Sky Queen and Sovereign
of the Skies rescues, the only two completely successful open
water ditchings in Commercial Aviation history.
Using the voices
of the passengers, flight crew, and the Cutter’s crewmen an
amazing tale unfolds. Their vivid memories, interspersed with contemporary
news reports, flesh out the unemotional entries from the cutter’s
logbook and official investigations.
No one flying, before or since,
ever experienced such harrowing rescues.


Excerpt from Chapter 6. Ditching : “Kick, kick, paddle,
paddle ….”
The Face of a Swell
Flying Tiger Line Lockheed Constellation Flight 923
560 Nautical Miles West of Shannon, Ireland
On September 23, 1962, at 10:00 P.M. Greenwich Mean Time, a Flying
Tiger Line Lockheed Super Constellation, under contract to MATS,
ditched at sea approximately 560 nautical miles west of Shannon,
Ireland. It carried 68 passengers and eight crewmembers. Of these,
24 passengers and four crewmembers died after the aircraft was in
the water.
The
passenger flight was from McGuire Air Force Base, New Jersey, to Frankfurt-Rhein
Main Airport, Germany, with a scheduled refueling stop in Gander, Newfoundland.
The original flight crew from McGuire was replaced by a new one in Gander.
The members on the Gander to Frankfurt leg consisted of Captain John D. Murray,
Copilot Robert W. Parker, Flight Engineer James E. Garrett, Jr., and Navigator
Samuel P. Nicholson. Stewardesses Elizabeth A. Sims, Carol Ann Gould,
Ruth Mudd, and Jacqueline L. Brotman were on board when the aircraft left McGuire
and remained with it on the leg from Gander to Germany.
Carol
Ann Gould was a last minute addition to the crew. She was staying with a friend
when, at 4:30 A.M. the phone rang, jolting her awake. It was an unexpected
call from the back office of Flying Tiger Airlines. Carol remembers the
conversation.
“We
need you to fill in for a stewardess who is sick. It will be double time,” said
the man from the back office of Flying Tiger Airlines.
“When
I got to the airport the head stewardess, Betty Sims, was beaming. She greeted
me warmly: ‘We know you’ve been out all night and you’re
tired, you can sleep. We just need your body on board to meet regulations. We
are heading over to McGuire Air base to pick up soldiers and take them to Germany.’”
The
aircraft departed McGuire AFB at 11:45A.M, with 68 passengers, including Army
paratroopers on their first overseas assignment, service members and their
families. Among these was Captain Juan G. Figueroa, an Air Force doctor, and
his wife, Carmen, who were going to Germany for a vacation.
Upon
departure the stewardesses briefed the passengers on over-water emergency procedures.
Between McGuire and Gander the navigator calculated his Equal Time Point (ETP)
and the Point of No Return (PNR) for the Gander-Frankfurt leg and placed these
on the appropriate navigational chart. These calculations were based upon the
weather information and weather charts provided by U. S. Air Force personnel
at McGuire AFB. The flight to Gander was routine. After the new flight crew
took over and refueling was completed, the aircraft took off at 5:09 P.M. on
the transatlantic leg of her journey.
At
7:20 P.M. the aircraft passed over the USCGC Owasco manningOcean Station
Charlie. John E. Ulibarri, a Radarman Second Class, was on duty and recalls:
“I
remember working Flight 923 and talking with the pilot, Captain John D. Murray. After
relaying Flying Tiger’s position, speed, and additional information,
Captain Murray wanted to know if I was interested in talking with the stewardess.
Being at sea for weeks at a time, I jumped at the chance to converse
with a female voice, a good distraction.
A
stewardess came on the radio and we joked back and forth for a couple of minutes.
‘Do
you sailors ever get lonely in the middle of the ocean?’ she inquired,
to which I replied, ‘Of course we do; there are no girls to talk to.’ When
she asked if talking to her helped, I told her that the only thing better would
be to be in the airplane with her. She laughed and said, ‘Maybe
next time.’
“We
signed off, and the flight continued east.”
Approximately three hours after departing Gander a fire developed
in the No. 3 engine. This engine was shut down and its propeller
feathered. A few minutes later the propeller of No. 1 engine
oversped when the flight engineer inadvertently closed the No. 1
engine firewall shutoff valve. This engine was also shut down and
the propeller feathered. At this time the captain altered course
to proceed to Shannon. After flying approximately one hour, the No.
2 engine developed trouble and the aircraft, with three bad engines,
was in serious trouble.
At
8:25 P.M., the aircraft requested sea conditions from Gander Radio. These were
later given by an eastbound DC-7 (identified by the call sign Riddle 18H) as
winds from 260 degrees at 28 knots; primary swells from 260 degrees, 8 to 12
feet high; secondary swells from 300 degrees, eight feet high.
The
requested escort aircraft, a U.S. Air Force C-118 four engine aircraft, piloted
by Lieutenant Joseph K. Lewis, and Riddle 18H were in visual contact shortly
before 9:00 P.M. About this time the No. 2 engine failed; however, its propeller
was not feathered. Captain Murray turned on the public address system and said: “Ladies
and gentlemen, this is the captain speaking. We are going to ditch.”
After
the second engine failure, the senior stewardess, Betty Simms, announced
over the loudspeaker system that they would conduct a ditching drill, at the
same time assuring the passengers that the aircraft could proceed to Shannon
on two engines. She then called attention to a ditching folder inside the pocket
behind each seat. The three remaining stewardesses circulated among the cabin
passengers and assisted in explaining the ditching procedure.
All
of the passengers donned lifejackets and were instructed not to inflate them
until they were outside the aircraft. None of the lifejackets were equipped
with lights.
Sometime
before ditching, two soldier passengers, at the direction of the crew, removed
the emergency liferaft stowed in the crew compartment and placed it in front
of the left rear main exit door where it was tied down. The door between the
crew compartment and the main cabin was removed and stowed in the left forward
coat closet. The stewardesses requested the passengers to remove dentures,
pens, pencils, glasses, and other sharp objects from their persons and to place
them in the pockets of the seatbacks.
Passengers
were asked if they had any knives or flashlights and those collected were then
distributed to certain passengers who had been given special duties such as
opening emergency exits and launching liferafts. According to the passengers,
most of the stewardesses did not have knives or flashlights, as required. Passengers’ shoes
and boots were also collected and these were stowed in the forward lavatory.
Many
paratroopers tried to act with bravado. One group filled plastic bags with
sandwiches and told stewardess Carol Gould to join them on their raft.
Shortly
before the ditching, Nicholson, the navigator, went into the cabin and removed
the tie-down strap from the liferaft. He then seated himself in an aisle seat
which was in the last row on the left side just forward of the main cabin door.
A
ditching heading of 265 degrees magnetic was then decided upon and C-118 was
alerted to stand by. Then Captain Murray turned to the left in order to obtain
the heading of 265 degrees.
Just
prior to impact Murray turned on the landing lights and cut the power on the
No. 4 engine. The plan was to land just past the top of a swell. However, just
before impact the nose of the aircraft was brought around parallel to the face
of the approaching swell and ditching was accomplished into the swell. After
initial impact, there were no skips or subsequent impacts.
The time was 11:12
P.M.
The
impact threw some passengers forward when seats broke loose. Water poured in
through the bottom of the plane. It was pitch black and little more than shadows
could be seen.
Captain
Murray’s head struck the instrument panel. He later recalled that the
copilot got out of his seat and asked him: “You all right John?” He
answered, "Yes.”
Murray
got up and followed the copilot and the flight engineer out of the cockpit
into the main cabin compartment. Upon reaching the cabin he remembered his
flashlight and went back into the cockpit and retrieved it. Returning from
the cockpit he said he observed the cabin to be clear of all persons. However,
he noticed some seats piled up in the rear of the cabin on the right side,
but blood in his eyes from a cut on his forehead prevented good vision.
Captain
Murray then left the aircraft through the forward left emergency over-the-wing
exit and inflated his lifejacket.
Nicholson
had some difficulty in opening the main cabin door. Wing exits were opened
easily with the exception of the aft over-the-wing exit on the right side,
which was opened after moving a seat which had partially blocked this exit.
Immediately after opening the main cabin door, Nicholson pushed out the liferaft,
but forgot to tie the lanyard provided for the liferafts’ retention to
the aircraft and the raft drifted away. Jumping in after it, he managed to
inflate it, although upside down with its emergency lights facing down.
One
survivor stated that he stood on the right wing after evacuating the cabin,
some recalled observing the right wing while exiting the aircraft, but other
survivors stated they saw no right wing.
During
the evacuation of the aircraft a few of the survivors said they could see clearly,
and others said they could hardly see at all. However, by following other
people they were able to find an exit. When the last passengers left the aircraft
the water inside was at least waist deep. A passenger who indicated that he
was the last one to leave said that he did not see anyone remaining in the
aircraft, although, he added, it was possible that some of the broken seats
may have concealed someone.
The
aircraft sank five minutes after impact.
In addition to the 25-man liferaft stowed in the crew compartment,
the aircraft carried four 25-man liferafts which were stowed in four
compartments, two in each wing aft of the rear spar. A cable control,
actuated by a handle located inside the jamb of the aft over-the-wing
exits, sequentially unlatches the wing compartments’ cover
doors and opens the valves to the CO2 cylinder of each raft on that
side of the aircraft.
As
each raft inflates it ejects itself automatically from the compartment. The
stowed rafts in the left wing can also be released by actuating a lever in
the cockpit. In addition to these releases there is a release mechanism on
each wing’s liferaft compartment.
None
of the liferafts stowed in the wings were seen by the survivors during the
evacuation; however, all rafts were later recovered. There was no evidence
that these rafts were used by any of the people who didn’t survive.
Meanwhile,
Carol Gould quickly removed the emergency window and shouted for the passengers
to follow her. She was anxious to drop down onto the left wing and open
the raft compartment door. As she looked down, she saw there was no wing; it
had sheared off on impact.
Twenty
foot waves pitched the survivors violently in and under the frigid water. One
huge wave swept Carol away from the plane while its undertow pulled Garrett
directly into the jagged edge of the broken wing, killing him instantly.
The
numbing cold and confusion left Carol in a coma-like state. The only clue she
was alive was the sound of her own heartbeat. She fought the urge to give up
and swam upward. As she broke through the debris-ridden surface Carol gulped
for air and cried out “I will not die this way.” She inflated only
the left side of her inflatable life vest, thinking she might need the other
side later.
The
survivors alternately swam and treaded water until they eventually found the
raft. Some said they saw a light, but it could not be established whether they
saw the automatically activated lights on the raft or the flashlight carried
by the captain. A total of 51 persons including Murray, Nicholson and Gould
swam to the raft and boarded it. As this number exceeded the capacity of the
raft by over 100 percent, the crowded conditions restricted movement.
Badly
overloaded, the raft took on water over the sides. Bailing was almost continuous
throughout the entire time on the raft and it was necessary for those on the
raft to hold the heads of others out of the water.
Somehow
the small grey raft remained intact. A few passengers had broken bones and
internal injuries. Many had second degree burns aggravated by the constant
chafing of their clothing as the waves buffeted them. Nearly all were suffering
varying degrees of shock and exposure.
Suddenly,
they heard propellers overhead as the C-118 swooped down and dropped a bright
red flare. Carol Gould remembered its eerie glow. “When it first dropped
it was like daytime on the raft. It was good, but it wasn’t. I
could see everyone around me and they were all bloody. The water in the raft
was turning a sickening red.
“Private
Brown was bleeding so badly from the big gash on his head that I knew something
had to be done. Then, I remembered my slip. I took it off and made a compress
out of it and put it on his head; then a wave washed it off. The only
way to keep it there was to hold it. He blacked out a few times.”
Aircraft
were overhead continuously from the time of ditching. Among them were three
Albatross amphibian search aircraft from Prestwick, Scotland. Originally their
pilots had hoped to land alongside any rafts they spotted, but the heavy seas
made this impossible. They were forced to head back to base for more fuel and
to get ready for another try.
Roughly
four hours later the small, 150-foot long Swiss freighter S. S. Celerina spotted
the raft after being directed to the scene by the C118.
Celerina’s
sailors threw rope ladders over the side, but by now the seas had reached 20
feet. At times the survivors were level with the deck of the vessel, only to
fall below the waterline the next moment.
From
the raft, Murray grabbed onto one ladder but fell back into the sea. Paratrooper
Fred Caruso grabbed him by the shirt and pulled him back into the raft. One
by one the exhausted survivors pulled their way up the ladders into the arms
of sailors.
Once
on deck, a sailor gave Carol a shot of whiskey and it warmed her. She searched
the deck for Doctor Figueroa and became his assistant, treating the wounded.
Passengers remember that she seemed to be everywhere, giving comfort and medicine.
Carol
paused only to look out to sea, hoping to glimpse another raft, hoping to find
her co-stewardesses. Betty had been sitting just behind Carol on the
plane. Her last words were to reassure Carol on how to retrieve the raft once
on the wing. “You will do fine, Carol, just fine.”
Throughout
the next hour Celerina’s crew continued rescuing survivors. No
one realized three people in the raft had died during the night: two servicemen
and a woman. The last man to exit the life raft had been holding his wife’s
body; she had perished during the night, he had not known.
Later
the sailors informed Carol that three empty rafts were picked up by other ships
in the area. Seven bodies were recovered near the ditch site, those of Stewardess
Brotman, Engineer Garrett, copilot Parker, and four servicemen. The other eighteen
were never found.
As
soon as he got aboard Celerina, Dr. Figueroa stripped off his clothing,
put on an old, greasy pair of pants and a shirt donated by a member of the Celerina’s
crew and went to work. He treated the injured, whose wounds ranged from severe
burns to deep slashes as well as shock and exposure.
Asked
in a interview how he kept going although himself a victim of the crash, he
modestly replied: “I don’t know. I guess it was a sense of duty
that kept me going. It was something that had to be done.”
The
doctor said he was too busy to stop, even though he had difficulty seeing—his
glasses were lost in the crash. “We worked with what we could find in
the ship’s emergency kit and a Canadian helicopter from the aircraft
carrier HMCS Bonaventure brought some supplies, but that proved to be
not enough. So then we had to have the air evacuation people take them off,” he
added.
Seventeen
of the most severely hurt were airlifted by helicopter off the ship to the
HMCS Bonaventure.
When
the aircraft ditched, Owasco, then 10 hours away, departed Ocean Station
Charlie and plowed through the night toward the crash site. Electricians Mate
Third Class Phil Gorman remembers: “I stood watch in my slicks
on the forward-most deck above the bridge in the rain and spray from the rough
water, staring into the wind and rain for hours.
At
6:00 A.M., September 24, Owasco arrived on scene. Electricians Mate
3rd Class Phil Gorman recalls: “The port bow watch spotted a yellow raft.
Out went a Monomoy life boat, which snagged a life raft. Nothing. The Mae West’s
were empty and that’s all there was in the raft. It didn’t make
sense. It was morning before anyone was found. The first, the body of the stewardess
who Ulibarri had been talking to was found floating face down. Then another
body, a young Marine [sic]. That was all.”
The
bodies on board Owasco were later picked up by a helicopter from Bonaventure and
taken to Scotland.
Stewardess
Ruth Mudd was on her last flight as a crew member after receiving notice from
the airline that she was being furloughed. Chief Stewardess Betty A. Sims,
married secretly two weeks before, had given notice this was her last trip.
Ruth Mudd’s body was not recovered. Carol Ann Gould was the only stewardess
to survive the ditching.
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